Been on a run out today about 60 miles or so. I thought the engine sounded a bit noisy so when I got home had a look and found the belt was loose, although hadn’t noticed the light come on so it wasn’t that loose. Removed the pulley wheel to investigate and I found that the inside half was cracked nearly all the way around the centre.
It’s been on for about seven years since the conversion from the old generator. Not sure why this has happened but I hope it’s a one off.
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It’s been on for about seven years since the conversion from the old generator. Not sure why this has happened but I hope it’s a one off.
Sent from my iPad using Tapatalk Pro