First drive from lockup to Nick's at CJ Motors for a nut and bolt check and fettle.
The running issues were solved by fitting the IDF40s off the old bus engine. So much easier with the hatch. Also had a sticky rocker, that was probably due to the engine sitting for such a long time before fitting.
Fairly successful apart from sitting stationary traffic for 1 1/4 hours and then being diverted through the back roads of Bedminster. Gear shift deteriorated rapidly, only left with 3rd and 4th.
Anyway, finally got to Redfield.
Saturday morning started well, poured a litre or so of ESSO E5 down my leg and into my boot whilst topping up the fuel level. Then as I went to move the bus out of the way so the workshop could be accessed there was a loud metallic noise and the gear shift went all floppy.
I reckon this could be the issue.
So back on axle stands again for a while.
Quick trip back across town to the lock up and came back with the CSP modified shift rod that was in the "parts that don't fit" box.
A bit of heating up and re-bending it finally sort of fitted.
While the front end was in the air, I found the top shock mounting nuts missing and the bolts just hanging so replaced those.
Other jobs done on the ramp, brakes re-bled much better now, fuel leaks sorted, and clutch conduit tube reattached to the torsion bar housing.
Drive home was uneventful, apart from the modified modified shift rod is fouling on the steering idler so 2nd gear is very hard to find.
Anyway, Barryfornia here we come.